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The Junkyard Turbojet Engine
A Real Working Jet Engine Built From Junkyard Parts!
Further developments of the turbine engine.The previous page related the steps involved in designing, building and testing a primitive turbine engine. That page has gotten quite long and cumbersome, so all further developments related to the engine will be posted here. This page has many photos and they will take a while to load.
11/03/99 After I was done dreaming, I went back to Copher's U-Pull-It just to have a look around. I had intended to just walk the yard looking for cars with turbos that are larger and in better shape than the one I have now. I didn't even take my tools with me. I intended to go back with tools in a day or two if I found something good. Imagine my surprise to see a perfectly good turbo charger sitting on the fender of a Thunderbird Turbo Coupe. Someone had needed the exhaust manifold. Naturally they had to first remove the turbo. I'm amazed they didn't take the turbo too, but just left it sitting there. It's larger than my first one, and the bearings seem to be in much better shape. I picked it up, walked briskly to the office, paid for it, and left before the other guy could decide he really wanted that turbo after all. I'm sure I can adapt the new turbo to all the rest of the parts fairly easily. I should really only have to make two new parts. A new flange with a new pattern of bolt holes drilled in it, and a new PVC air pipe. Only minor modifications to the test stand should be needed. I'm in no real hurry to rebuild the engine with the new turbo. I want to experiment a little with the first turbo. I also need to demonstrate the engine to some more people before I take it all apart. ![]() This is my second turbo charger. It was found sitting on the fender of a Thunderbird Turbo Coupe in the scrap yard. I didn't even have to get greasy pulling it off the engine. 11/05/99 I ran a piece of 1/8 inch copper tubing down the inlet of the turbo until it almost touches the compressor wheel, and clamped it in place. The end of the tubing is bent at what seems like the best angle for spinning up the wheel. I also mounted an air valve in a convenient spot near the rest of the engine controls. Now starting the engine with compressed air is dead easy. Even my wimpy little air compressor can do it. As a fringe benefit, The sound made by the air impinging on and spinning up the compressor wheel is really impressive. Now my little engine really sounds like a jet engine. If you close your eyes you could swear you are standing next to an F16 starting up it's engine. 11/09/99 ![]() The flame tube after about 1 hour of total runtime. Badly discolored but otherwise ok. I also tore down the oil filter/cooler assembly to find and fix an annoying and messy oil leak that has been driving me nuts. I installed new O rings and made a new gasket from silicone gasket material. this seems to have solved the problem. When I reassembled the engine I used high-temp silicone gasket material between the flange and the adaptor plate and between the adaptor plate and the turbo. This has stopped the hot air leaks I was experiencing. 11/10/99 About 30 minutes into the run I heard the engine start to slow down. It was a very gradual spool down. I came running to see what was going on. The fuel pressure was dropping and I at first assumed I had run out of propane. Then I saw all the ice on the propane tank. The tank was so cold that the internal pressure was rapidly dropping toward zero. Only about a pound of propane had been burned according to my not very sensitive scale, but all that ice probably masked some weight loss from the tank. I shut down the engine and decided to table this particular project until I find a way to prevent this problem. 11/13/99 - 11/14/99
![]() Here you can see the cooling tubing wrapped around various parts of the combustor just before I mummified it with layers of aluminium tape to improve heat transfer. The 3 wraps on the far left are to pre-heat the oil and reduce it's viscosity before it goes to the turbo. I ran the engine quite a bit this weekend. It is not running as well as it did in the beginning. The turbo bearings seem to be getting worse with every run. It now sometimes starts wobbling at only 3.5 psi of boost. I am also seeing a lot of oil in the cooling water discharged from the turbo. I am afraid the time is coming soon when I will have to retire this turbo charger and install the new one. I spent some time this weekend working on the new flange that will mate to the new turbo. 11/20/99 Although my guests were impressed, I was not. The engine was running very badly, and I couldn't throttle it up very high at all. It was also leaking oil worse than ever. I think this is the end for the poor tired old turbo charger. Tomorrow I will install the new turbo. 11/21/99
![]() This is the new larger turbo charger. It's a Warner-Ishi IHI Turbo from an 86 Thunderbird Turbo Coupe. The long black spring on the right side is holding the wastegate shut. Above about 6 psi there are occasional events that seem like little backfires. I suspect that this is the infamous compressor surge I have heard about. I will probably try bleeding off some compressor air to see if that helps the problem. I included a large air tap in the new air pipe I had to build to mate the new turbo to the existing combustor. I have plans to use some compressor air anyway to attempt to run some accessories. I also found that the engine is now much harder to start on compressed air, especially when it's cold. It can take two or three tries to start the cold engine, but it will usually restart on the first try when it's already hot. This is probably just because the turbo is bigger and my air compressor is so small and wimpy. Someday I just have to buy a more "macho" air compressor. 11/23/99 I want to replace the AC motor driving the oil pump and make the engine independent of outside power sources once it has been started. A couple of weeks ago I bought a small centrifugal blower with the idea of modifying it to operate as an air motor that would run off of compressor bleed air. I removed it's electric motor and set about making modifications. Tests using shop air showed that the completed motor spins at outrageous speed, but produces very little torque. I next built a gear train to reduce the speed and increase the torque. The finished unit was tested on bleed air from the running engine today. The unit works, but I'm still not sure it will produce enough torque to run the pump, especially at low boost pressures. I will do a test run soon with the unit actually driving the pump. If it doesn't work, I'll rework the gear train. I have also been trying to get rid of the annoying "backfires" or surging I'm seeing at high boost pressures. I first tried bleeding off some compressor air. This didn't seem to help much. I also tried some different injectors, but they all worked much worse than the original. One of them produced some really impressive "wet" starts that made my engine act like a flame thrower. Too bad I didn't get any photos. I went back to the original injector and started messing with the air holes in the flame tube. I found that opening up the 4 air holes immediately next to the injector a little bit helped. I also found that letting the engine warm up for a while at low speed before throttling up to wide open also helped smooth out the running. I must have started the engine 2 dozen times in the last two days. I'm getting quite good at starting it on the first try with compressed air even when it's cold. I think the problem was that I wasn't opening the fuel valve far enough fast enough. With the new turbo installed the engine is now quite a fuel hog. It took me a while to learn that I really have to give it the juice to get it going. 11/24/99 ![]() Here you can see the air motor I built to run the oil pump. The air comes through the black hose from an air tap in the pipe that delivers air from the compressor to the combustor. ![]() This is another view of the air motor driving the oil pump. Now my engine only needs compressed air and 12 volts (AC or DC) to start. Once running all umbilicals except cooling water can be removed and it will keep going as long as I feed it fuel. Someday I will close the cooling loop and then I will have something that is close to being able to move under it's own power. I'm thinking maybe go-cart. I also have a friend who builds and flys ultra light aircraft. Hmmm...Somebody stop me. 11/26/99 11/27/99
![]() This is the new nozzle made from standard pipe fittings. Here it still has the tubing for the failed propane heat exchanger wrapped around it. Giddy with the success of the nozzle, I then embarked on another experiment. I wrapped about 10 feet of 1/4 inch tubing around the nozzle and clamped it on tight to create a heat exchanger for vaporizing liquid propane. The heat exchanger worked a little too well. The propane got so hot that the copper tubing all the way to the pressure regulator (about 3 feet) is badly discolored. The hot propane damaged the regulator and started melting the hose downstream from the regulator. Aside from the excess heat, I also saw a surging problem with the propane pressure. It looks to me like the liquid propane gets to the heat exchanger where it flashes into high pressure vapor. The high pressure vapor then drives the liquid back into the tank and sends a pressure pulse toward the regulator. The pressure then drops and allows more liquid into the heat exchanger and the cycle repeats. The surges were coming about 1 a second. Obviously I'm supplying way too much heat to the propane, but on the bright side, the tank pressure did not drop during the run. ![]() Another view of the engine with the new nozzle and propane vaporizer in place. The upside down propane tank can just barely be seen behind the test stand. 11/28/99 12/11/99 ![]() Here is a view of the engine with the propane vaporizing heat exchanger installed. See text for a description In operation the liquid propane passes through the double tube to the loops around the nozzle where it gets heated to a very high temperature and vaporizes. The hot propane vapor passes back through the double tube and is cooled down to a safe temperature by the cold liquid in the other tube, preheating it in the process. The gradual preheating of the liquid propane in this system seems to have eliminated the pressure surges I was getting with the other heat exchanger. I start the engine on propane gas. After about a minute when the nozzle is good and hot I turn the propane tank upside down and start feeding the engine liquid propane. This system works very well. I have run the engine for as long as 15 minutes at a moderate boost level with no appreciable drop in the propane tank pressure. In the past the pressure would start to drop after only a few minutes and the engine would start to slow down. I should now be able to do the long duration run I wanted to do a month ago to measure the rate of fuel consumption. Now that I have solved the fuel pressure problem, I need to work on a new fuel injector that will get more fuel into the engine. 12/14/99 I put the old injector back in and ran a few tests. It's been cool lately, and my propane tanks are cold. This means the maximum propane pressure I have to work with is 100-110 psi. With the present fuel injector in place the engine tops out at 7 psi of boost at full fuel pressure. I can do better on a warm day when the tanks have more pressure in them, but even in summer I doubt I'll be able to go much beyond 10 psi of boost with this injector and only tank pressure. A higher flow injector and more air holes in the flame holder should help increase power, I hope. Being limited by the propane tank pressure has got me thinking about liquid fuel. The ability to pump in fuel at whatever pressure I choose is an exciting prospect. I'm leaning toward diesel just because it's so easy to obtain. I bought some misting nozzles from McMaster Carr a while ago. Now I'm going to be looking for a high pressure fuel pump. Someday I'll get it all together. 12/24/99 I decided that it's time to make a new flame tube out of stainless steel. I found some inexpensive stainless tubing at Don's Salvage Yard. I don't know what type of SS it is, but I'm going to hope it works better than the steel electrical conduit the first one was made of. 12/26/99 I spent the rest of the day fabricating and testing different fuel injectors. I now have a very large collection of fuel injectors that don't work very well, or at all. I am now working with a design suggested by Chris Krug. I don't have the necessary tools to exactly duplicate his design, but I am trying to make something similar. My first attempt worked, but not very well. The engine would only run up to about 4 psi of boost. Attempting to throttle up beyond 4 psi resulted in lots of popping, coughing, and momentary flameouts. My second attempt had similar results, but I can see potential in this design. The two injectors tested today worked better than most others I've tried. I think the problem is that my engine is smaller than Chris' and the new injectors are simply providing too much fuel. I'll try drilling out some with fewer and/or smaller orifices another day. It's cold outside, the propane pressure is low, I'm tired, and it's time to watch football. 02/08/2000 Today I found some great pieces of stainless steel scrap at Don's Salvage Yard. They should be perfect for building a new large diameter combustor and flame holder. Total cost $30. I think his price is way too high, but the parts are so perfect for the job that I bought them anyway. I'll post photos of the new parts soon. The time I spent working on the engine last year put me behind on other projects. Progress on the engine will probably be slow for a while until I get caught up with other things. 05/19/2000 I unscrewed the nozzle and fired up the engine again. This time there was no measurable thrust even at full throttle. The nozzle is obviously very important for generating thrust. I suspect that a proper nozzle instead of my jury-rigged one may produce even more thrust. I'll need to look into getting one made. 2.5 pounds of thrust probably wouldn't push a lightly loaded bicycle across smooth and level ground. Even with a proper nozzle I doubt I'll get much more thrust on propane. The pressure in the propane tank is the limiting factor. I really need to find the time to work on the conversion to liquid fuel. Stay tuned for future developments. |
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